BeckerFraserPhotos March 2012 photograph 149
Images, UC QuakeStudies
Photograph captioned by BeckerFraserPhotos, "Substantial site development in Kennedys Bush Road, near the intersection with School Road".
Photograph captioned by BeckerFraserPhotos, "Substantial site development in Kennedys Bush Road, near the intersection with School Road".
Photograph captioned by BeckerFraserPhotos, "Substantial site development in Kennedys Bush Road, near the intersection with School Road".
A pdf copy of a post from the One Voice Te Reo Kotahi blog. The post is titled, "NGO delegate developments and more to discuss at Tuesday's forum!".
Photograph captioned by BeckerFraserPhotos, "Substantial site development in Kennedys Bush Road, near the intersection with School Road".
A poster in Kaiapoi showing the estimated timeframe for, and location of, likely residential land developments in Kaiapoi, the wider Waimakariri District and in the rural residential areas, based on major planning and subdivision applications with the Waimakariri Council as at February 2012.
During the Christchurch earthquake of February 2011, several midrise buildings of Reinforced Concrete Masonry (RCM) construction achieved performance levels in the range of life safety to near collapse levels. These buildings were subjected to seismic demands higher than the building code requirements of the time and higher than the current New Zealand Loadings Standard (NZS-1170.5:2004). Structural damage to these buildings has been documented and is currently being studied to establish lessons to be learned from their performance and how to incorporate these lessons into future RCM design and construction practices. This paper presents a case study of a six story RCM building deemed to have reached the near collapse performance level. The RCM walls on the 2nd floor failed due to toe crushing reducing the building’s lateral resistance in the east-west direction. A nonlinear dynamic analysis on a 3D model was conducted to simulate the development of the governing failure mechanism. Preliminary analysis results show that the damaged walls were initially under large compression forces from gravity loads which caused increase in their lateral strength and reduced their ductility. After toe crushing failure developed, axial instability of the model was prevented by a redistribution of gravity loads.